ON TUESDAY MARCH 1ST 1960 SEVERAL ROYAL AIR FORCE MEN WERE
BEING REPATRIATED TO THE UNITED KINGDOM AFTER THEIR TOUR OF DUTY IN THE FAR
EAST, THESE MEN WERE MAINLY STATIONED AT ROYAL AIR FORCE STAGING POST KATUNAYAKE
(KNOWN BY ALL AS KAT) IN CEYLON, THERE WERE TWO ROYAL MARINES
AND TWO ABLE SEAMEN FROM THE ROYAL NAVY ALSO RETURNING TO THE UNITED KINGDOM.
TOGETHER WITH THE COMMANDING OFFICER OF KAT, WING COMMANDER GEOFF ATHERTON
D.F.C. AND A FLIGHT LIEUTENANT FROM PAY ACCOUNTS THESE SERVICEMEN MADE UP
THE COMPLEMENT OF 14 PASSENGERS WAITING TO BOARD A HANDLEY PAGE HASTINGS TG579
A C1 AIRCRAFT OF 48 SQUADRON CHANGI, SINGAPORE FOR THE 600 MILE TRIP TO ROYAL
AIR FORCE GAN IN THE MALDIVE ISLANDS.
THE HASTINGS WAS DELAYED FOR A LONG PERIOD OF TIME DUE TO
TECHNICAL PROBLEMS, ALTHOUGH STEW AND TONY THINK THE CREW MAY HAVE MADE A
RETURN TRIP TO GAN THAT DAY AND WE SHOULD HAVE BEEN EN ROUTE TO GAN BY MID
MORNING, HOWEVER DUE TO THESE DELAYS THE PASSENGERS AND CREW DID NOT EMBARK
UNTIL 1700HRS LOCAL TIME AND EVENTUALLY LIFTED OFF FROM RAF KATUNAYAKE AT
1734HRS. THE KNOWN PASSENGERS WERE CORPORALS BILL GRUNDY A FIREMAN, (BILL)
MURRAY AN ENGINE FITTER, SENIOR AIRCRAFTSMEN TONY GREEN AIRFRAME MECHANIC,
STEWART TUCKER AIR RADAR MECHANIC, TONY MEALING AIR WIRELESS MECHANIC(?),
DAVID BLOOMFIELD AN MT DRIVER AND JOHN GARY COOPER AN ENGINE MECHANIC,
LEAVING ONE PASSENGERS NAME WE CANT REMEMBER.
THE CREW NUMBERED SIX, THE CAPTAIN AND FIRST PILOT WAS FLIGHT
LIEUTENANT R.T.D. SCOTT A HIGHLY EXPERIENCED PILOT WITH OVER 3000 FLYING HOURS
ON HASTINGS AIRCRAFT ALONE AND WAS A HOLDER OF A MASTER GREEN INSTRUMENT RATING
CERTIFICATE, HIS CO-PILOT WAS FLIGHT SERGEANT G.F. APPLEGARTH MUCH LESS EXPERIENCED
ON TYPE WITH APPROXIMATELY 500 FLYING HOURS, I AS A PASSENGER UP TO THIS DATE
HAD 97 HOURS FLYING EXPERIENCE IN HASTINGS AIRCRAFT. THE REMAINDER OF THE
CREW CONSISTED OF A NAVIGATOR, SIGNALLER, FLIGHT ENGINEER AND AIR QUARTERMASTER
(LATER KNOWN AS LOADMASTER) WHOSE NAMES ARE UNKNOWN.
THE WEATHER ON LIFT OFF WAS FINE AND STILL DAYLIGHT, THIS
AIRCRAFT, APART FROM ITS PASSENGERS, WAS CARRYING SOME AIRCRAFT GROUND EQUIPMENT
IN THE FORM OF AIRCRAFT HYDRAULIC JACKS AND THE EQUIPMENT NECESSARY TO EQUIP
THE DENTAL SECTION AT RAF GAN IN THE AIRCRAFTS FUSELAGE AND ALSO PERSONAL
EFFECTS OF THOSE ON BOARD IN THE LUGGAGE HOLD, THE PASSENGERS HAND LUGGAGE
WAS SITUATED IN RACKS STOWED ABOVE THE PASSENGERS HEADS. I WAS SAT FACING
AFT ON THE STARBOARD SIDE OF THE AIRCRAFT ADJACENT TO A PORT HOLE WINDOW AND
DIAGONALLY OPPOSITE THE MAIN PASSENGER DOOR, A MATE AND WORK COLLEAGUE TONY
GREEN, SAT ALONG SIDE ME, WE WERE TAKING PHOTOGRAPHS OF THE LAST IMAGES OF
CEYLON AND THOSE BRILLIANT SUNSETS ENCOUNTERED IN THAT PART OF THE WORLD,
CHATTING ABOUT GOING HOME AFTER TWO PLUS YEARS AND LOOKING FORWARD TO A GOOD
OLD ENGLISH PINT OF BEER.
IT WASNT LONG BEFORE IT GOT DARK AND THERE WAS SOME
TURBULENCE, WHICH IS USUALLY FOUND ON MOST AIRCRAFT TRIPS, THIS TURBULENCE
INCREASED IN INTENSITY OVER A PERIOD OF TIME, WE WERE INFORMED TO FASTEN SEAT
BELTS AS RECALLED BY TONY, AND ON APPROACH TO GAN THE TURBULENCE WAS EXTREMELY
SEVERE, I MYSELF HAD NEVER ENCOUNTERED SUCH BUFFETING AS THIS BEFORE, LIGHTNING
COULD EASILY BE SEEN LIGHTING UP THE CLOUDS, ONE WONDERS WHY THE PILOT CANNOT
FLY ABOVE THE STORM BUT OFTEN CLOUD BANKS IN INTENSE TROPICAL STORMS CAN RANGE
FROM A FEW HUNDRED FEET ABOVE SEA LEVEL TO HEIGHTS OF OVER 30000 FEET, THIS
HASTINGS AIRCRAFT DID NOT HAVE THIS CEILING CAPACITY AND TO MY KNOWLEDGE DID
NOT CARRY OXYGEN OR MASKS FOR SUCH AN EVENTUALITY ( ALTHOUGH SOME HASTINGS
WERE FITTED WITH MASKS AND OXYGEN ESPECIALLY WHEN USED IN THE CASEVAC ROLE)
, NORMAL FLYING HEIGHT WOULD BE APPROXIMATELY 8000 FEET FOR A TRIP OF THIS
SORT. IT IS INTERESTING TO NOTE THAT AT GAN THE AIRFIELD MEASURES JUST OVER
ONE MILE SQUARE AND THE LENGTH OF THE SINGLE RUNWAY EQUALS THE EXACT LENGTH
OF THE ISLAND WITH NO UNDER OR OVERSHOOT FACILITIES (APART FOR SOFT CORAL
BELOW THE HIGH AND LOW TIDE WATER LEVEL), THERE ALSO WAS (IN 1960) NO OTHER
AIRFIELD WITHIN HUNDREDS OF MILES OF GAN TO DIVERT TO IN THE EVENT OF AN EMERGENCY,
APART FROM A RETURN TRIP TO KATUNAYAKE AND THERE WOULD HAVE BEEN ENOUGH FUEL
ON BOARD THE AIRCRAFT TO MAKE THIS RETURN TRIP IF DEEMED NECESSARY.
AS PASSENGERS WE WERE ALL GETTING PRETTY ANXIOUS, SOMETHING
I HAD NEVER EXPERIENCED BEFORE WITH FLYING IN BOTH CIVIL AND MILITARY AIRCRAFT,
WHEN SUDDENLY THE LIGHTS OF GAN AIRFIELD APPEARED BELOW THE AIRCRAFT, SOME
EYE WITNESSES (CORPORAL ANDY MUTCH AN AIR WIRELESS FITTER OF SASF GAN AWAITING
THE ARRIVAL OF THE AIRCRAFT) COULD HEAR THE AIRCRAFT BUT NOT SEE IT DUE TO
THE EXTREME WEATHER CONDITIONS PREVAILING, OTHERS INCLUDING MIKE BUTLER COULD
SEE THE AIRCRAFT AND ESTIMATED ITS HEIGHT AT 80, I FELT THE HEIGHT WAS
400, WE KNOW FROM THE OFFICIAL ACCIDENT REPORT THAT THE CLOUD BASE WAS
420 AND THAT THE HASTINGS OVERSHOT THE RUNWAY, STEWART AND TONY THOUGHT
THE AIRCRAFT DID TOUCH THE RUNWAY, DAVID AND I AM CERTAIN IT DID NOT, OTHERS
CLAIMED THAT THE AIRCRAFT FLEW IN FROM THE WEST (FEDHOO DIRECTION) INCLUDING
FIREMAN ROGER STEVE STEVENS WHO WAS IN CHARGE OF THE FIRE STATION
THAT NIGHT AND WHO HAD TAKEN UP A POSITION ADJACENT TO AIR TRAFFIC CONTROL
WITH HIS CREW IN THE FIRE ENGINE WHICH IS NORMAL PROCEDURE, IT IS KNOWN THAT
THE AIRCRAFT MADE ONE SINGLE LOW LEVEL APPROACH, EXACT HEIGHT UNKNOWN, OVER
THE ISLAND FROM THE EAST AND BANKED TO PORT. THE ACCIDENT REPORT RECORDS THIS
TIME AS BEING 2034 HOURS LOCAL TIME, EXACTLY THREE HOURS AFTER LIFT OFF FROM
OUR HOME BASE IN CEYLON, (THESE TIMES WERE ORIGINALLY QUOTED ZULU
TIMES AND HAVE BEEN READJUSTED TO LOCAL TIMES FROM CORPORAL HARRY HEYWOOD
STATIONED IN GAN AIR TRAFFIC CONTROL THE NIGHT OF THE INCIDENT AND EX SQUADRON
LEADER NEIL JONES AN EXPERIENCED EX HASTINGS AND HERCULES TRANSPORT PILOT).
HASTINGS TG579 FLEW OFF FOR ANOTHER TWENTY MINUTES AND ACCORDING
TO THE ACCIDENT REPORT MADE A VERY LONG LOW APPROACH TO LAND IN MARGINAL
WEATHER CONDITIONS IT WAS AT THIS POINT THAT THE WEATHER WAS STILL RAGING,
WHEN WITHOUT ANY WARNING THERE WAS A MIGHTY CRASH AND JUDDERING AND SILENCE
FROM THE ENGINES, IT IS KNOWN THAT THE UNDERCARRIAGE WAS DOWN AND ON THIS
FIRST IMPACT BECAME DETACHED FROM THE HASTINGS, BOTH WHEELS STILL INFLATED,
WERE RECOVERED THE FOLLOWING MORNING BY THE MARINE CRAFT SECTION WHEN FOUND
TO BE AFLOAT DRIFTING IN THE LAGOON, THESE WERE RETRIEVED BY ROD VENNERS USING
A DAVID BROWN TRACTOR. IT IS THOUGHT THAT ON THIS FIRST IMPACT AT 125 KNOTS
THAT NUMBERS ONE AND TWO HERCULES ENGINES WERE TORN OUT OF THE BEARERS AND
DETACHED FROM THE BULKHEADS, WE KNOW THAT THESE TWO ENGINES WERE DEFINITELY
MISSING, IT IS ALSO THOUGHT THAT NUMBER THREE ENGINE ALSO BECAME DETACHED
AS REPORTED BY ALL FOUR SURVIVING PASSENGERS. DEFINITELY NUMBER FOUR ENGINE
WAS STILL ATTACHED. ALSO AT THIS POINT IT IS THOUGHT THAT THE AIRCRAFT SWUNG
ROUND 180 DEGREES FROM ITS EASTERLY APPROACH AND WAS NOW FACING AWAY FROM
GAN (TG580 CRASHED ON LANDING AT GAN IN JULY 1959 AND PREVIOUS TO THIS TWO
OTHER INCIDENTS INCLUDING ONE ON THE GREENLAND ICECAP INVOLVING A HASTINGS,
EACH TIME THE AIRCRAFT SWUNG 180 DEGREES), A FURTHER THEORY IS THAT THE GAN
CHANNEL WHERE THE HASTINGS CAME DOWN IN THE SEA, THAT THE CURRENT HERE FLOWS
AT A VERY FAST 7-8 KNOTS AND IT IS THOUGHT POSSIBLE THAT THE AIRCRAFT SWUNG
ROUND ON THE CURRENT. NEXT THERE WAS ANOTHER CRASH, NOT AS SEVERE AS THE FIRST
BUT TOO HARD FOR ANY NORMAL LANDING IT WAS AT THIS POINT THAT A FIRST AID
BOX BECAME DETACHED FROM ITS STOWAGE FLEW ACROSS THE CABIN AND HIT GEOFF ATHERTON
FULLY IN THE FACE, WE LATER DISCOVERED THIS BROKE HIS NOSE. THERE THEN WAS
A THIRD ALMOST GENTLER CRASH ALMOST AS THOUGH THE AIRCRAFT HAD LANDED ON THE
RUNWAY. I DISTINCTLY REMEMBER LOOKING OUT OF THE WINDOW AND SAYING TO TONY
GREEN THAT I COULD NOT SEE ANY RUNWAY LIGHTS (T0NY RECALLS THIS EVENT), IT
WAS NOT OBVIOUS TO ANY OF THE PASSENGERS AT THAT TIME BUT WE HAD HIT THE SEA
AND OUR FIRST KNOWLEDGE OF THIS WAS WHEN THE AQM OPENED THE MAIN ENTRANCE/EXIT
DOOR WHEN WATER RUSHED IN. HERE WE WERE HAVING JUST CROSSED THE EQUATOR BY
SOME 41 MILES AND OUR BAPTISM WAS ABOUT TO BE REALISED.!
ON THE ACCIDENT REPORT ON THIS FINAL LOW LEVEL APPROACH TO
THE RUNWAY THE REPORT READS ON THE SECOND APPROACH THERE WAS A BRILLIANT
FLASH OF LIGHTNING AT ABOUT 2 MILES, CAUSING PILOT TO LOOK INTO COCKPIT TO
RECOVER HIS VISION. SECOND PILOT THEN CALLED APPROACHING 50 AND ALMOST
IMMEDIATELY AIRCRAFT HIT THE SEA. MINOR INJURIES WERE SUSTAINED BY ALL MEMBERS
OF CREW AND PASSENGERS (INCIDENTALLY FROM BOTH BLOOMFIELD AND COOPERS
MEDICAL RECORDS THERE IS NO MENTION OF THIS). IT ALSO SEEMS INCREDIBLE THAT
A TRANSPORT AIRCRAFT OTHER THAN A FLYING BOAT WOULD BE FLYING AT THIS LOW
ALTITUDE FROM SUCH A DISTANCE FROM THE RUNWAY (1.5 NAUTICAL MILES), THE CLOUD
BASE WAS WE KNOW 420 AND LATER A SHACKLETON MR1 DID A SARAH (SEARCH
AND RESCUE AND HOMING), AND THERE IS NO WAY THAT THE SHACKLETON WOULD HAVE
BEEN SEARCHING AT THIS ALTITUDE.
IN AIR TRAFFIC CONTROL HARRY HEYWOOD RECALLS THE EVENING
THAT THE HASTINGS DITCHED TO THE EAST OF THE ISLAND, I WAS ON DUTY IN THE
ATC TOWER. IT WAS A QUIET EVENING WITH LITTLE ACTIVITY ON THE W/T CIRCUITS
AND I WAS CHATTING TO THE DUTY CONTROLLER, FLIGHT LIEUTENANT MORGAN-SMITH,
WHEN THE HASTINGS MADE HIS FIRST APPROACH THROUGH THE GALE AND LASHING RAIN
THAT ENVELOPED THE ISLAND. THE AIRCRAFT ABORTED ITS INITIAL APPROACH AND ASKED
FOR THE RUNWAY LIGHTS TO BE INCREASED IN INTENSITY. THIS WAS DONE, AND WE
STROVE TO SEE HIS LANDING LIGHTS THROUGH THE STORM, BUT IT WAS IMPOSSIBLE-IT
WAS LIKE A SCENE FROM A HOLLYWOOD MOVIE. THE DATCO ASKED HIM (THE PILOT) TO
CONFIRM THREE GREENS - UNDERCARRIAGE DOWN AND LOCKED - AND THE
LAST TRANSMISSION WAS HIS ANSWER, ROGER, DOWNWIND, THREE GREENS, RUNWAY
IN SIGHT.
SUDDENLY THERE WAS WHAT APPEARED TO BE A FEEDBACK SCREECH,
PERHAPS TWO MICROPHONES BEING OPENED AT THE SAME TIME, AND THE C/R D/F (CATHODE
RAY DIRECTION FINDER) REACTED TO IT. THE TRACE ILLUMINATED ON THE SCREEN,
ORIENTATED EAST, THE DIRECTION WHERE HE (THE AIRCRAFT) WAS EXPECTED TO BE.
THE DATCO (DUTY AIR TRAFFIC CONTROL OFFICER) INITIATED A CALL; NO REPLY; CALLED
AGAIN, NO REPLY, AND EXCLAIMED, CHRIST, I THINK HES GONE IN
OR WORDS TO THAT EFFECT. AT THAT POINT CONTROLLED PANIC TOOK OVER AS THE SAR
(SEARCH AND RESCUE) DRILLS WERE PUT INTO EFFECT, AND I KEPT OUT OF THE WAY.
I HAVE A SUSPICION THAT ONE OF MY WIRELESS OPERATORS SENIOR AIRCRAFTSMAN RUSS
TAYLOR , ON HIS OWN INITIATIVE HAD MADE HIGH FREQUENCY RADIO TRANSMITTER CONTACT
WITH THE BOATS (AIR SEA RESCUE LAUNCHES)
ROGER STEVENS, IN CHARGE OF THE GAN FIRE STATION WAS ALONGSIDE
THE CONTROL TOWER WHEN INSTRUCTED TO ENTER THE ACTIVE AND PROCEED WITH
CAUTION, BECAUSE WE THINK THE AIRCRAFT HAS CRASHED. ROGER AND HIS CREW
WERE DISPATCHED TO THE CHANNEL END OF THE ISLAND TO SEARCH FOR THE AIRCRAFT
AND SURVIVORS BUT FOUND OR HEARD NOTHING. THEY WERE ALSO INSTRUCTED TO WADE
OUT ON TO THE CORAL REEF BUT DECIDED AGAINST THIS COURSE OF ACTION DUE TO
THE PRESENCE OF SHARKS AND MORAY EELS IN THE VICINITY. HOWEVER THE SASF DUTY
CREW WERE TAKEN BY VEHICLE TO THIS POINT AND DID WADE ON TO THE REEF TO LISTEN
AND SEARCH FOR SURVIVORS BUT AGAIN FOUND AND HEARD NOTHING, THE STATION ADJUTANT
STOOD THE DUTY CREW DOWN AND GAVE THEM A BOTTLE OF RUM FOR THEIR EFFORTS AS
RECALLED BY ANDY MUTCH. ALL EMERGENCY TEAMS ON STANDBY WERE CALLED OUT,
BY GREAT FORTUNE A SEARCH AND RESCUE SHACKLETON MR1 AIRCRAFT OF 205 SQUADRON
INDEX NUMBER WB834 HAD BEEN DETACHED FROM CHANGI ON A TWO WEEK ATTACHMENT
TO GAN AND THIS AS FAR AS WE HAVE BEEN INFORMED WAS AIRBORNE WITHIN 20 MINUTES
OF THE ACCIDENT OCCURRING. FLIGHT LIEUTENANT JOHNNY ELIAS WAS THE DUTY CAPTAIN
AND FIRST PILOT. BILL BARKER WAS ON THE PINNACE 1374 (ASR LAUNCH) AS A SENIOR
AIRCRAFTSMAN MOTOR BOAT CREWMAN AND WAS DISPATCHED TO THE SCENE OF THE DITCHING,
INCIDENTALLY THIS LAUNCH CAN STILL BE SEEN PLYING THE WATERS AROUND THE HOLYHEAD
AREA.
BACK AT THE CRASH SITE, ORGANISED CHAOS WAS TO BE SEEN, WITH
THE SUDDEN SURGE OF WATER INTO THE FUSELAGE AREA EVERYONES IMMEDIATE
REACTION WAS TO VACATE THE SINKING HASTINGS AS QUICKLY AS POSSIBLE, I CERTAINLY
RECALL TAKING MY LAP BELT OFF, REACHING IMMEDIATELY ABOVE MY HEAD TAKING THE
MAE WEST (LIFE JACKET) FROM ITS PLYBOARD STOWAGE, BEING AT LEAST ANKLE DEEP
IN WATER, BUTTONING UP THE JACKET BUT NOT TIGHTENING THE STRAPS AND EXITING
THE AIRCRAFT BY THE MAIN DOOR (I HAVE SINCE BEEN INFORMED BY FRANK OGDEN AN
EX HASTINGS FLIGHT ENGINEER THAT IF INFLATING A LIFE JACKET BEFORE ENTERING
THE WATER THERE WAS A GOOD CHANCE OF BREAKING YOUR NECK WHEN ENTERING THE
SEA !), AT THIS POINT THERE WAS NO THOUGHT OF SALVAGING ANY OF OUR PERSONAL
POSSESSIONS, IT WAS A QUESTION OF SAVING LIVES THAT BECAME THE PRIORITY. IT
IS CLAIMED BY PILOT OFFICER COLIN VINCENT WHO WAS POSTED TO HQFEAF FAIRY POINT,
CHANGI SHORTLY AFTER THE CRASH AND WAS A SERVING NATIONAL SERVICE OFFICER
ATTACHED TO THE LEGAL BRANCH, SEEING THE BOARD OF INQUIRY REPORTS AND RECALLS
THAT HE HAD MET WING COMMANDER GEOFF ATHERTON ON A NUMBER OF OCCASIONS AT
FAIRY POINT AND RECALLED THAT HE WAS A MOST CHARMING AND COURTEOUS MAN
AND THAT IT WAS GEOFF THAT TOOK CHARGE IN HIS CALM AUTHORITATIVE MANNER WHICH
ENSURED THAT THE PASSENGERS EXITED THE AIRCRAFT INTO LIFE RAFTS IN AN ORDERLY
MANNER, THAT ALL THE CREW WERE ALSO SAFE AND THAT RAFTS WERE KEPT TOGETHER
UNTIL RESCUED BY THE HIGH SPEED LAUNCH I WOULD LIKE TO MENTION AT THIS
POINT THAT NO INSTRUCTIONS WERE HEARD BY THE FOUR SURVIVING PASSENGERS ON
EVACUATING THE AIRCRAFT, SOME MEMBERS OF CREW AND SOME PASSENGERS EXITED THE
AIRCRAFT VIA THE MAINPLANE ESCAPE HATCHES AND STEPPED INTO THE INFLATED DINGHIES,
WHILST AT LEAST ALL FOUR PASSENGERS MENTIONED EARLIER WERE IMMERSED IN SEA
WATER, FUEL AND OIL WHEN VACATING THE AIRCRAFT. I ALSO RECALL OTHERS IN THE
WATER, IT WAS EXTREMELY DIFFICULT TO HAUL MYSELF INTO A DINGHY, AS I HAD INGESTED
A LUNG FULL OF WATER, OIL AND FUEL, ONCE IN THE WATER I PULLED MY RED EMERGENCY
TOGGLE ON MY LIFE JACKET AND THIS BROUGHT ME TO THE SURFACE, I ESTIMATE MY
TIME IN THE WATER AT LESS THAN FIVE MINUTES, IM NOT SURE, BUT I WAS
PULLED ON A LIFERAFT BY A SAILOR OR MARINE AS I CERTAINLY ENDED UP IN THEIR
DINGHY. STEW TUCKER HELD ON TO HIS LIFE JACKET UNTIL HE GOT INTO THE DINGHY
AS HIS BUTTONS WERE ALREADY FASTENED UP,TONY ALSO RECALLS THE BUTTONS BEING
FASTENED WHEN TAKEN FROM THE STOWAGE, DAVID BLOOMFIELD RECALLS HAVING TO FIGHT
OFF SOMEBODY HAMPERING HIS PROGRESS TO GET INTO A DINGHY.
ONCE WE WERE ALL IN THE DINGHIES A HEAD COUNT WAS ORDERED
BY A FLIGHT LIEUTENANT PAY ACCOUNTS OFFICER FROM KATUNAYAKE AND STEW TUCKER
TOOK ON THIS ROLE GIVING EACH PERSON A NUMBER, HE RECALLS NUMBERING HIMSELF
LAST, IT WAS AT THIS POINT THAT A MEMBER OF CREW HAD BEEN REPORTED MISSING
AND WE COULD CERTAINLY HEAR CRIES OF HELP FROM WHAT APPEARED TO BE THE STARBOARD
SIDE OF THE AIRCRAFT, IT IS THOUGHT BY ALL THAT THIS WAS THE FLIGHT ENGINEER
WHO HAD EITHER ESCAPED THROUGH THE EMERGENCY HATCH NEXT TO HIS STATION OR
VIA THE STARBOARD WING, IT IS KNOWN THAT OF THE 20 OCCUPANTS ALL ESCAPED THROUGH
EXITS ON THE PORT SIDE OF THE AIRCRAFT EXCEPT THE ONE PERSON ADRIFT. IT WAS
AT THIS POINT THAT GEOFF ATHERTON DIVED INTO THE WATER FROM A DINGHY AND SWAM
AFTER THE PERSON WHO WAS ADRIFT. HE STAYED WITH THIS PERSON UNTIL RESCUED
DESPITE RECEIVING THE FULL FORCE OF A WOODEN FIRST AID BOX FULLY IN HIS FACE
SUSTAINING A BROKEN NOSE, WE UNDERSTAND THAT GEOFF ATHERTON WAS AWARDED A
COMMENDATION FOR HIS DEEDS THAT NIGHT AND JUSTLY DESERVED. IT IS ALSO NOTEWORTHY
TO REPORT THAT GEOFF SHOT DOWN 5 JAPANESE BOMBERS AND FIGHTERS IN WW2 AND
WAS AWARDED THE DFC AND BAR, HE WAS EVENTUALLY SHOT DOWN BY THE JAPANESE INTO
THE SEA IN 1944 AND WAS RESCUED BY A CATALINA FLYING BOAT. SO TWICE HE ENDED
UP IN THE DRINK!
SEVERAL MINUTES HAD PASSED SINCE THE INITIAL DITCHING AND
WE WERE ABLE TO COLLECT OUR THOUGHTS AND PUT IN TO BEING A PLAN OF ACTION,
THE FIRST THING NECESSARY WAS TO GET OURSELVES AWAY FROM THE AIRCRAFT AS QUICKLY
AS POSSIBLE FOR SEVERAL REASONS, WHEN THE HASTINGS WAS GOING TO SINK WOULD
THE SUCTION TAKE US DOWN AS WELL, THERE WAS THE ADDED RISK OF HIGH OCTANE
AVGAS FUEL AND ENGINE OIL IGNITING PLUS OTHER HAZARDS OF BATTERY ACIDS AND
OTHER VOLATILE SUBSTANCES IN THE AREA. IT WAS AT THIS POINT THAT WE HAD FOUND
SOME PADDLES IN THE DINGHIES AND I CERTAINLY WAS USING ONE OF THESE FRANTICALLY
TRYING TO PADDLE THE DINGHIES AWAY FROM THE TWISTED ALUMINIUM OF THE WINGS
AND TAILPLANE, STEW RECALLS HOW HE HAD LEFT THE DINGHY BY STEPPING ON TO A
WING TRYING TO PUSH THE DINGHIES AWAY FROM THE AIRCRAFT, WHAT WE DID NOT KNOW
WAS THAT THE DINGHIES WERE STILL TETHERED TO THE AIRCRAFT BY CORD, STEW RECALLS
IT WAS ME THAT HAD SPOTTED THIS AND ASKED IF ANYONE HAD GOT A KNIFE, WHEN
EITHER A SAILOR OR MARINE PULLED A KNIFE FROM HIS SOCK AND SEVERED THE CONNECTIONS,
THE REMAINDER OF THE CORD WAS THEN USED TO TETHER THE DINGHIES TOGETHER, NONE
OF US ARE SURE HOW MANY DINGHIES WERE IN USE BUT THE CONSENSUS OF OPINION
IS THAT THERE WERE THREE, ONE OF WHICH WAS DEFLATING (PROBABLY PUNCTURED BY
THE ALUMINIUM), ONE WHICH CONTAINED THE CREW NO ONE RECALLS HOW THIS BECAME
DETACHED FROM THE OTHER TWO.
FORTUNATELY THERE WAS LIGHT FROM THE EMERGENCY BATTERIES LIGHTING
UP THE INSIDE OF THE FUSELAGE AND FLASHES OF LIGHTNING STILL RAGING FROM THIS
HORRENDOUS STORM, SO WE WERE AT TIMES ABLE TO SEE WHAT WAS GOING ON APART
FROM FEELING AROUND THE DINGHIES FOR EMERGENCY EQUIPMENT. WE HAD CERTAINLY
FOUND THE PADDLES AND AT LAST WE WERE MAKING PROGRESS IN GRADUALLY DRIFTING
AWAY FROM THE POINT OF DANGER, HOWEVER THE DINGHY THAT WAS DEFLATING WAS CAUSING
SOME ANXIETY TO ITS OCCUPANTS AS CORPORAL MURRAY, A RATHER ROTUND CHAP, WAS
BEING PHYSICALLY ILL AND SITTING ON THE BELLOWS AS RECALLED BY TONY, DAVID
AND STEW, THEY EACH TOOK IT IN TURNS BY KEEPING THE DINGHY INFLATED BY THIS
PUMPING ACTION. BOTH DAVID, STEW AND I RECALL FINDING HATS, TO
ALL INTENTS AND PURPOSES THESE LOOKED LIKE A HUGE TEAT END PIECE OF A CONDOM,
THIS CONSISTED OF A PLASTIC TIGHT FITTING HOOD WITH A TINY TORCH BULB IN THE
TEAT END, TO ACTIVATE THE LIGHT YOU HAD TO IMMERSE A SMALL CIGARETTE SIZE
PACKET BATTERY IN WATER (OBVIOUSLY WE HAD AN OCEAN FULL OF THIS!) WHICH ACTIVATED
THE LIGHT BULB ON THE TOP OF THE HEAD, THERE WERE MANY OF THESE IN THE DINGHIES
BUT HOW THESE COULD BE SEEN FROM ANY DISTANCE IS BEYOND ME. WE NEVER CAME
ACROSS ANY OTHER EQUIPMENT WITHIN THESE DINGHIES, TO MY KNOWLEDGE THERE SHOULD
HAVE BEEN EMERGENCY RATIONS INCLUDING DOG BISCUITS, DRIED HORLICKS
TABLETS AND OTHER TABLETS TO CONVERT SALT WATER IN TO FRESH WATER, IN ADDITION
THERE SHOULD HAVE BEEN A YELLOW BOX KITE (FOR DAY TIME USE) AND FLARES BUT
NONE OF THESE WERE FOUND. DAVID RETAINED HIS HELIOGRAPH FROM HIS MAE WEST,
THIS IS A SIGNALLING DEVICE EMPLOYING A QUADRANT MIRROR TO REFLECT THE SUNS
RAYS FOR PASSING SHIPS AND AIRCRAFT TO SPOT IN SUCH EMERGENCIES.
AGAIN ONLY MINUTES HAD PASSED FOR ALL OF THIS TO HAPPEN, WE
COULD HEAR THE ENGINES OF THE SHACKLETON FIRE INTO LIFE AND TO A TRAINED MECHANIC
THIS SOUND OF 4 ROLLS ROYCE GRIFFON ENGINES WAS ALMOST HEAVEN SENT, WE AS
SURVIVORS DIDNT KNOW THERE WAS A SHACKLETON BASED AT GAN BUT MIGHTY
PLEASED THAT THERE WAS.
WE WERE NOW BEGINNING TO SETTLE DOWN INTO SOME SORT OF ROUTINE
WITHIN THE DINGHIES, WE WERE NOW WELL ADRIFT OF THE CRASHED HASTINGS WHICH
WAS STILL AFLOAT, PERHAPS TWO HUNDRED YARDS AWAY FROM ITS TAIL END, THE NOSE
POINTING AWAY FROM GAN (AS ALSO REMEMBERED BY STEW , DAVID AND MYSELF), THE
AIRFIELD LIGHTS WERE TO OUR RIGHT AND WE COULD ONLY SEE THESE AS WE ROSE ON
THE CREST OF EACH GIANT WAVE, HANGING ON TO THE GUIDE ROPES FOR DEAR LIFE,
STILL IN A RAGING THUNDERSTORM. HOW TG579 MANAGED TO RIDE THESE WAVES FOR
SO LONG IS A REMARKABLE TESTAMENT TO ITS DURABILITY AGAIN IT IS A CONSENSUS
OF OPINION THAT SHE STAYED AFLOAT FOR SOME TWENTY MINUTES UNTIL SLIPPING DOWN
STARBOARD WING FIRST (STEW THINKS PORT WING DOWN) INTO DEEP WATER. THE PORT
WING ROSE INTO THE AIR DEVOID OF BOTH OF ITS HERCULES ENGINES, OTHERS NOTICED
THAT NUMBER THREE ENGINE WAS ALSO MISSING, IT WAS SAD TO SEE HER DISAPPEAR
AS SAILORS WOULD A SINKING OR TORPEDOED SHIP. IT COULD HAVE EASILY BEEN US
GOING DOWN WITH IT, I ALSO FIND IT AMAZING THAT IF TWO OR THREE ENGINES WERE
RIPPED FROM THE BULKHEADS WEIGHING OVER A TON EACH WHY THE WINGS WERE NOT
TORN OFF ON THE FIRST IMPACT I CANNOT IMAGINE WHY THEY DIDNT, PERHAPS
THE SLOW LANDING SPEED PREVENTED THIS AND WITH THE THREE CRASHES IT WOULD
APPEAR AS IF THE AIRCRAFT SKIPPED THE SEA LIKE A PEBBLE SKIPPING ACROSS THE
TOP OF A POND.
ONCE TG579 HAD SLID BELOW THE WAVES, IT WAS TIME TO TAKE STOCK,
STEW TUCKER SUGGESTED THAT EVERYONE REMOVED THEIR SHOES AND BOOTS TO PREVENT
ANY MORE DINGHIES BEING DEFLATED FROM SHARP OBJECTS LIKE EXPOSED NAILS OR
STUDS OR BLAKEYS, SOME SHOES WERE THROWN OVERBOARD TO STOP CLUTTERING
UP THE DINGHIES, THOSE THAT WERE RETAINED WERE KEPT ON THE OWNERS LAP IN CASE
WE HAD TO USE THESE FOR BALING OUT WATER FROM THE DINGHIES. THERE WAS WATER
IN ALL THE DINGHIES BUT IN MINE NOTHING TO WORRY ABOUT, IT WAS PROBABLY RESIDUAL
WATER FROM THE RAIN OR SEA WATER SPLASHING OVER THE HIGH WALLS OF THE LIFE
RAFTS.
THE SHACKLETON WAS BY NOW AIRBORNE AND A SYSTEMATIC SEARCH
WAS STARTED AS RECALLED BY HARRY HEYWOOD THE FLARES WERE CLEAR POINTS
OF LIGHT, NOT FUZZY AS THEY WOULD HAVE BEEN IF FALLING THROUGH CLOUD. THE
SHACKLETON WAS RUNNING IN ON THE RUNWAY LINE FIRING OFF SINGLE FLARES ONE
AFTER ANOTHER, THEN AS HE PASSED OVER THE DITCHED HASTINGS HE WOULD FIRE OFF
A CLUSTER, PULL AWAY THEN REPEAT THE PROCEDURE. FROM A PASSENGER POINT
OF VIEW THIS APPEARED TO BE WHAT I RECALLED, BUT THE HASTINGS WOULD HAVE BEEN
ON ITS WAY OR ON THE BOTTOM OF THE SEA BED BY THIS TIME. SHACKLETON AIRCRAFT
HAD SOPHISTICATED RADAR ON BOARD AND CARRIED A CREW OF TEN, DESPITE THE FACT
THAT NO METAL OBJECT WAS ON THE SURFACE (TG579) THIS WOULD HAVE BEEN QUITE
EASY TO DETECT AS IF THE HASTINGS WERE A SUBMARINE, I AM NOT AWARE THAT ANY
ASDIC OR SONAR BUOYS OR OTHER SIMILAR EQUIPMENT WAS BEING USED BY THE SHACKLETON.
AT THIS POINT DON ELLIS THE FIRST NAVIGATOR ON THE OFF DUTY SHACKLETON AT
GAN FROM 205 SQUADRON CHANGI RECALLS THE THE ATROCIOUS TROPICAL STORM AND
ASKED THE OPERATIONS OFFICER WHAT THE CREW OF THE HASTINGS SHOULD DO , THE
OPS OFFICER REPLIED IF THEY HAD ANY SENSE THEY WOULD RETURN TO KATUNAYAKE.THE
C.O. OF GAN, WING COMMANDER EWAN THOMAS WAS IN AIR TRAFFIC CONTROL WITH THE
DUTY AIR TRAFFIC CONTROL OFFICER. THE CREW OF THE HASTINGS DID A BLIND APPROACH
BEACON SYSTEM (BABS) APPROACH ALMOST RELIANT UPON INSTRUMENTS. DON LATER RECALLS
THE HASTINGS NAVIGATOR CALL 2 MILES AND THE CO-PILOT SAYING
YOURE DOWN TO 50. AIR TRAFFIC CONTROL THEN HEARD NOTHING
AND WONDERED IF THE AIRCRAFT HAD LOST RADIO CONTACT AND SO THE RESCUE TENDER
(FIRE ENGINE) WAS SENT TO TRAVEL THE LENGTH OF THE RUNWAY TO SEE IF THE HASTINGS
WAS ON THE GROUND. THE SEARCH AND RESCUE SHACKLETON CAPTAINED BY JOHNNY ELIAS
WAS DESPATCHED TO THE END OF THE RUNWAY TO SHINE ITS LIGHTS LOOKING FOR THE
AIRCRAFT, JOHNNY THOUGHT THAT IF HE WAS TO DO THIS HE MIGHT AS WELL HAVE GOT
AIRBORNE SO WITHIN 10 MINUTES THEY WERE ON THE RUNWAY THRESHOLD. THE AIRCRAFT
TOOK OFF AND STARTED FIRING FLARES FROM 3 MILES TO 2 MILES OUT FROM THE CRASH
SCENE ON THE FIRST RUN AND THEN RUNNING IN FROM 2 MILES THEY SPOTTED WRECKAGE
AND DINGHIES WHERE THE TWO AIR SEA RESCUE LAUNCHES WERE DESPATCHED TO THE
SCENE. DONS AIRCRAFT TOOK TO THE AIR THE NEXT MORNING LOOKING FOR WRECKAGE
AND SAW A MAIN WHEEL AFLOAT, THE LAUNCHES LATER COLLECTED THESE. DON ALSO
RECALLS THAT HE TOOK GEOFF ATHERTON BACK TO KATUNAYAKE IN HIS SHACKLETON AS
GEOFF REFUSED POINT BLANK TO FLY BACK IN A HASTINGS!
THE MORALE IN THE DINGHIES WAS VERY GOOD, THERE WAS PLENTY
OF SHOUTING AND SINGING, THE USUAL CHESTNUTS OF WHY ARE
WE WAITING, SHOW ME THE WAY TO GO HOME ETC WERE ALL BEING
SUNG, THE FLARES WERE GETTING EVER CLOSER AND THAT WE SOMEHOW KNEW THAT THE
CHANCES OF RESCUE WERE EXTREMELY HIGH, SOME WAG SUGGESTED WHAT WOULD HAPPEN
IF ONE OF THE FLARES ENTERED THE DINGHY, HOW HE DIDNT GET FED TO THE
SHARKS IS ANYONES GUESS! IT WAS APPARENT AFTER SOME WHILE THAT THE SHACKLETON
HAD FOUND US AS THE FLARES WERE FALLING IN AN ARC SOME DISTANCE FROM THE DINGHIES
AND THIS WAS TO GUIDE THE TWO RESCUE LAUNCHES TO THE CRASH SITE.
WE COULD SEE SOME DISTANCE AWAY BRIGHT LIGHTS, THESE WERE
A MIXTURE OF THE GAN AIRFIELD LIGHTS AND WE EVENTUALLY SPOTTED SEARCH LIGHTS
SEEMINGLY LIKE A VERY LONG WAY AWAY, THESE WERE ONLY VISIBLE AS WERE THE AIRFIELD
LIGHTS WHEN WE WERE APPROACHING THE CREST OF A WAVE. AT THIS POINT IN TIME
WE DID NOT KNOW WHERE WE HAD DITCHED, WE KNEW WE WERE TO THE EAST OF GAN AIRFIELD
AND WOULD ESTIMATE AS BEING BETWEEN ONE AND TWO MILES OUT WHAT I DIDNT
KNOW UNTIL APRIL 2001 WAS THAT THIS AREA IS TREACHEROUS IN THAT IT IS KNOWN
AS THE GAN CHANNEL AND SEPARATES TWO ISLANDS WILLINGILI TO THE EAST AND GAN
ISLAND TO THE WEST THIS STRETCH OF WATER IS WHERE THE CALMER LAGOON OF THE
ADDU ATOLL MEETS THE INDIAN OCEAN WITH THE TIDAL WATERS RUNNING VERY FAST
AS RECALLED BY BRIAN BARKER , AT ABOUT EIGHT KNOTS.
BRIAN WAS ON PINNACE 1374 THE SMALLER OF THE TWO RESCUE LAUNCHES,
I CANNOT RECALL SEEING THIS BOAT BUT BRIAN RECALLS PICKING UP WING COMMANDER
GEOFF ATHERTON AND ONE OTHER (THE FLIGHT ENGINEER?) PLUS ANOTHER DINGHY LOAD
WHO WE ASSUME TO BE THE OTHER CREW MEMBERS, WE THINK THIS PINNACE ARRIVED
BACK TO THE GAN JETTY AFTER THE LARGE LAUNCH PICKED UP THE PASSENGERS AND
I AM INFORMED BY STEW THAT THE AQM WAS WITH THE PASSENGERS. THERE WAS MUCH
REJOICING WHEN THE LARGER LAUNCH WAS APPROACHING US, SHOUTING BY ALL, THE
WAVING OF ARMS ALL HELPED TO KEEP THE MORALE HIGH. THIS LAUNCH LOOKED HUGE
IN COMPARISON TO OUR DINGHIES AND AS IT GOT EVER NEARER THE SWELL LOOKED EVEN
WORSE AS THERE WAS A BACKWASH BETWEEN THE GROUP OF DINGHIES AND THE LAUNCH.
SCRAMBLING NETS WERE ATTACHED TO THE SIDE OF THE LAUNCH AND IT WAS WITH GREAT
DIFFICULTY TO HOLD ON TO THE ROPE AND THEN PUT ONES FEET ON THE ROPE, IF YOUVE
EVER CLIMBED A LADDER WITH SOFT SOLED SHOES ON YOU CAN APPRECIATE OUR PLIGHT,
RAGING SEAS, HUGE SWELL COVERED IN FUEL AND OIL BUT I WAS IN GOOD HANDS AS
ONE OF THE MARINE CRAFT GUYS LITERALLY GRABBED THE BACK OF MY MAE WEST AND
HAULED ME UP ON DECK, WHERE DAVID RECALLS BEING PULLED ABOARD BY HIS HAIR!
I WAS IMMEDIATELY TAKEN BELOW DECK AND GIVEN A BLANKET AND TOWEL AND A MUG
OF TEA WHICH I DRANK AND IMMEDIATELY BROUGHT BACK UP AGAIN WITH A CONCOCTION
OF OTHER FLUIDS IN MY MOUTH. I STILL REMEMBER THOSE MATTRESSES WITH A TICKING
STRIPE COVER AND FEELING VERY MUCH THE WORSE FOR WEAR, PERHAPS IT WAS PART
EMOTION THAT BROUGHT THIS ON, I HAD NEVER SUFFERED FROM TRAVEL SICKNESS BEFORE
OR SINCE , THAT WAS AN EXCEPTION. STEW RECALLS THE HULL OF THE LAUNCH SCRAPING
THE CORAL, THIS MUST HAVE BEEN SOMEWHERE NEAR THE REEF AREA LATER AS OUR IMMEDIATE
RESCUE WAS FROM DEEP WATER. IT MUST BE MENTIONED HERE THAT A HEARTFELT THANK
YOU MUST GO TO THE OFFICER COMMANDING THE MARINE CRAFT SECTION FLIGHT LIEUTENANT
BERNIE SAUNDERS, HIS COXSWAIN DICKIE DENMAN FOR THE BRAVERY SHOWN THAT NIGHT
AND THE CREWS OF THOSE TWO MOTOR LAUNCHES WHO SET SAIL IN THE WORST POSSIBLE
WEATHER CONDITIONS PREVAILING AT THAT TIME AND IN CURRENTS SO STRONG THAT
UNDER NORMAL CONDITIONS THEY WOULD NOT VENTURE OUT THROUGH THE REEF AREA EXCEPTING
IN DIRE EMERGENCIES, I UNDERSTAND THAT A COMMENDATION WAS AWARDED TO BERNIE
SAUNDERS THAT NIGHT AND AGAIN, JUST LIKE GEOFF ATHERTONS AWARD, RICHLY
DESERVED.
IT IS UNDERSTOOD BY VARIOUS PARTIES THAT WE WERE IN THE DINGHIES
FOR 1 1/2 HOURS, I HAVE ALWAYS MAINTAINED THAT TO BE CORRECT, OTHERS THINK
LONGER, CERTAINLY THE PINNACE ARRIVED AFTER THE LARGE LAUNCH AND THAT IT IS
THOUGHT THE CREW AND THOSE OTHER TWO ADRIFT ARRIVED ABOUT AN HOUR LATER. ROGER
STEVENS RECALLS HE GAVE ASSISTANCE AT THE JETTY BY LIGHTING UP THE AREA WITH
THE FIRE ENGINE LIGHTS AND RECALLS THE FIRST PERSON HE HAD HELPED ASHORE WAS
A CORPORAL BILL GRUNDY WHO HE HAD PREVIOUSLY SERVED WITH AT RAF BALLYKELLY,
IT IS ALSO INTERESTING TO NOTE THAT ANOTHER SURVIVOR ROGER HELPED ASHORE WAS
A SAILOR WHOSE COMMENTS WERE THIS IS THE FIRST TIME IVE FLOWN
WITH THE RAF AND THEY TRIED TO DROWN ME, SOMETHING THAT THE NAVY NEVER DID
!
JOHN BAWDEN WHO WORKED IN GAN AIR TRAFFIC RECALLS THAT WE
WERE TAKEN TO THE STATION SICK QUARTERS AND APART FROM ONE OR TWO THAT HAD
INGESTED FUEL AND OIL THAT NO OTHER SERIOUS INJURIES WERE SUSTAINED. JOHN
TRAVELLED BACK TO LYNEHAM ON THE WHITE KNUCKLE BRITANNIA RIDE
THE NEXT DAY AT KARACHI, I REALLY DO NOT RECALL COMING OFF THE LAUNCH AND
HOW I GOT TO SICK QUARTERS (WITHOUT ANY SHOES ON), BUT I DO RECALL BEING MEDICALLY
EXAMINED, OTHERS SAY THEY WERENT AND BEING PASSED FIT TO FLY TO THE
UK THE NEXT DAY. I IMAGINE THAT I WAS GIVEN FRESH KD CLOTHING THAT NIGHT AT
GAN BUT AGAIN I CANT REMEMBER, I DO REMEMBER NOT BEING ABLE TO SLEEP.
IT WAS IN STATION SICK QUARTERS THAT THE CREW WERE BROUGHT IN AND THERE WAS
MUCH ANIMOSITY FROM THE PASSENGERS TOWARDS THE PILOT, IN THE FORM OF VERBAL
ABUSE AND FINGER WAGGING, I REALLY CANNOT REMEMBER THIS HAPPENING BUT I CAN
ACCEPT WHY IT DID OCCUR.
I AM ALSO INFORMED THAT WITH WHAT FEW RUPEES WE HAD LEFT BETWEEN US THAT WE
CLUBBED TOGETHER AND BOUGHT THE SHACKLETON RESCUE CREW A BOTTLE OF WHISKEY
TO SHARE AMONG HIS CREW AND AS A THANK YOU., AGAIN WITHOUT THEIR ASSISTANCE
WHO KNOWS WHAT THE OUTCOME WOULD HAVE BEEN.
THE FOLLOWING MORNING WEDNESDAY 2ND MARCH 1960 I RECALL QUEUING
FOR SOME EMERGENCY PAY AS ALL MY LEAVE MONEY WAS IN MY CAMERA BAG, £35=0=0
PAID IN 10/= NOTES AT RAF KATUNAYAKE, A KINGS RANSOM IN THOSE DAYS (ABOUT
£700-800 POUNDS TODAY), THE REASON WE WERE ALL PAID IN BROWN 10/= NOTES
WAS THAT PAY ACCOUNTS HAD RUN OUT OF WHITE FIVERS AND BLUE POUND NOTES!
ALL OF THAT MONEY AND MY PERSONAL POSSESSIONS WERE LOST IN THAT ACCIDENT,
THE ONLY THING THAT I WAS ABLE TO SALVAGE WAS MY OMEGA SEAMASTER WATCH WHICH
WAS ON MY WRIST. WHEN I ASKED THE MARINE CRAFT BOYS WHAT EFFECTS WERE FOUND,
THEY SAID NOTHING APART FROM THE WHEELS OF THE HASTINGS, I AM SURE IT WAS
THEY THAT TOLD ME THAT THE AIRCRAFT HAD SUNK TO A DEPTH OF OVER 1000 FATHOMS
WHILST DAVID BLOOMFIELD WAS TOLD THIS DEPTH BY A MEMBER OF THE SHACKLETON
CREW, IT DOESNT REALLY MATTER WHAT DEPTH IT ENDED UP IN WE LOST EVERYTHING.
ALL FOUR PASSENGERS SAY THEY LOST EVERYTHING INCLUDING LEAVE PAY AND STEW
TUCKERS DEEP SEA BOX WAS ON BOARD THE HASTINGS GIVING A NEW MEANING TO THE
TERM DEEP SEA BOX!
I FEEL REMARKABLY LUCKY THAT THE AIRCRAFT STAYED AFLOAT AND
DIDNT BREAK UP ON IMPACT AND THAT THE INJURIES SUSTAINED WERE OF A MINOR
NATURE TO ALL. I AM ALSO FORTUNATE THAT WE DIDNT KNOW WHAT WAS ABOUT
TO UNFOLD AND THAT THE PILOT DIDNT KNOW WHAT WAS ABOUT TO HAPPEN TO
HIS AIRCRAFT, IF EITHER OF THE ABOVE WAS KNOWN THEN I AM SURE THAT THE CIRCUMSTANCES
WOULD HAVE BEEN COMPLETELY DIFFERENT. AS AN ENGINE MECHANIC I HAD NO PARTICULAR
LOVE AFFAIR FOR A HASTINGS AIRCRAFT, THEY WERE REASONABLY EASY TO SERVICE
AND QUITE RELIABLE AS PISTON ENGINED AIRCRAFT BUT TOOK SOME TIME TO TURN
AROUND. HAVING SAID THAT THE DESIGN TEAM OF A HANDLEY PAGE HASTINGS
DESIGNED PERHAPS THE BEST AND MOST DURABLE NON FLYING BOAT AIRCRAFT THE ROYAL
AIR FORCE TOOK DELIVERY OF AS ANOTHER HASTINGS CRASHED IN THE MEDITERRANEAN
OFF CASTEL BENITO AIRFIELD AND ENDED UP FLOATING FOR SOME TIME FOR ALL ON
BOARD TO MAKE THEIR ESCAPE.
CREDIT MUST GO TO ALL THOSE THAT TOOK PART IN THE RESCUE,
THEY WERE ALL HEROES, ON THE NIGHT THEY DID THERE DUTY THAT THEY WERE TRAINED
TO DO IN APPALLING WEATHER CONDITIONS AND NOT KNOWING WHETHER THEY WERE LOOKING
FOR SURVIVORS OR BODIES OR EVEN NOTHING IF THE AIRCRAFT HAD SUNK WITHOUT TRACE,
AND IT IS TO THESE PEOPLE THAT I SAY A MIGHTY BIG THANK YOU!
THE HISTORY OF TG579 READS THUS:
CONTRACTOR HANDLEY PAGE LTD, CRICKLEWOOD, CONTRACT NUMBER 4186, ENGINES INSTALLED
4 BRISTOL HERCULES 101 AIR COOLED RADIAL ENGINES.
TYPE HASTINGS C1 RAF NUMBER TG579
12/04/1949 CONTRACT COMPLETED
13/04/1949 TO 241 OPERATIONAL CONVERSION UNIT (OCU)
08/10/1949 TO LYNEHAM
18/10/1951 HANDLEY PAGE FOR MODIFICATIONS UNTIL 01/11/1951 AND RETURNED TO
LYNEHAM ON THAT DAY
05/02/1953 TRANSFERRED TO RAF TRANSPORT COMMAND AIR SUPPORT FLIGHT (ASF)
02/03(?)/1955 TO 29 MAINTENANCE UNIT
08/03/1956 TO 242 OCU
18/08/1956 TO ROS/60 MU
23/08/1956 EX ROS
03/06/1957 20 MU
06/12/1957 FREE LOAN FOR ONE MONTH
07/01/1958 20 MU
20/01/1958 TRANSFERRED TO 48 SQUADRON FEAF (CHANGI)
01/03/1960 FLYING ACCIDENT CATEGORY 5
08/03/1960 STRUCK OFF CHARGE
TG579 FINALLY HAD HERCULES 216 ENGINES ADDED SOMETIME IN ITS LIFE A.M. FORM
78 DOES NOT RECORD THE DATE.
THE OFFICIAL ACCIDENT REPORT AS PROVIDED BY THE AIR HISTORIC BRANCH AT RAF
BENTLEY PRIORY WAS HAND WRITTEN AND THIS HAS BEEN DECIPHERED BY SQUADRON LEADER
NEIL JONES AND WARRANT OFFICER (THEN CORPORAL AT GAN) HARRY HEYWOOD, THE OFFICIAL
BOARD OF INQUIRY WAS HELD AT HQ FEAF FAIRY POINT CHANGI, SINGAPORE, DATE UNKNOWN
BUT HELD BEFORE MAY 1960.
IT IS WITH MANY THANKS TO ALL WHO HAVE PAINSTAKINGLY SHOWN
AN INTEREST FOR MY SEARCH FOR THE TRUTH, YOU HAVE PROVIDED, IN MANY CASES,
THE MISSING PARTS OF THE JIGSAW.
SINCE THE NIGHT OF THIS ACCIDENT IVE ALWAYS WANTED TO
KNOW WHY OUR LIVES WERE IN SUCH DANGER, I ALWAYS HAD A SNEAKING SUSPICION
THAT SOMETHING WAS AMISS AND I COULDNT GET TO THE BOTTOM OF IT, I (AND
DAVID BLOOMFIELD TOO )HAD STROVE TO ASK QUESTIONS TO THE VARIOUS AUTHORITIES
WITHIN THE THEN AIR MINISTRY AND LATER MINISTRY OF DEFENCE AND NOTHING WAS
FORTHCOMING. I BASICALLY KEPT THIS LITTLE EPISODE TO MYSELF AND
ONLY MY WIFE AND CLOSEST FRIENDS KNEW THE BARE BONES OF THAT NIGHT,
I KEPT THESE THOUGHTS TO MYSELF FOR OVER 40 YEARS, HAVING MANY FLASHBACKS
AND SLEEPLESS NIGHTS, SWEATS AND NERVOUS TENSION. (I NOW KNOW THAT I AM NOT
THE ONLY ONE!) I HAD NO AMBITION OF FURTHERING MY CAREER IN THE WAY OF PROMOTION
TO THE NON COMMISSIONED RANKING SYSTEM I STAYED A JUNIOR TECHNICIAN ENGINE
FITTER UNTIL MY DISCHARGE. MY DIARIES FROM 1962 TO 1969 SHOW MY INTENSE HATRED
FOR THE ROYAL AIR FORCE AND RECORD ON NUMEROUS OCCASIONS REQUESTS ON GENERAL
APPLICATION FORMS TO OBTAIN A DISCHARGE, BUT THE ONLY WAY OUT WAS BY PURCHASING
MY CONTRACT OF EMPLOYMENT BACK FROM THE AIR MINISTRY AND ON EACH OCCASION
AMOUNTED TO £200 WHICH I COULD NOT AFFORD, SO I RODE OUT
MY TWELVE YEARS BEGRUDGINGLY. I ENJOYED MY WORK AT THE SHARP END
ENORMOUSLY, THE COMRADESHIP OF THE LOWER RANKS APPEALED TO ME MORE THAN THE
HIGHER RANKS, APART FROM SOME EXCEPTIONS THERE WAS ALWAYS AN AIR OF ALOOFNESS
PREVALENT, HOWEVER I MET THIS LESS WHEN IN FIGHTER COMMAND.
MY QUEST WAS ANSWERED IN MARCH 2001, ALMOST EXACTLY 41 YEARS
ON, TO GET TO THE TRUTH, I FIRSTLY BOUGHT MYSELF A COMPUTER IN JANUARY 2001
AND SURPRISINGLY IT DID NOT TAKE ME LONG TO GET USED TO IT. I SURFED
THE NET DAY AND NIGHT FOR ADDRESSES AND EYE WITNESSES AND ALL OF THIS
WAS READILY AVAILABLE, I PLACED TWO SEARCHES ON CHANNEL 4S SERVICE
PALS PAGES IN JANUARY AND MARCH FOR EYE WITNESSES AND WAS WELL PLEASED
WITH THE RESPONSE AND EVEN PEOPLE WHO WERENT INVOLVED KNEW SOMEONE THAT
WAS! THE INFORMATION I ASKED FROM OFFICIAL SOURCES WAS SLOW IN COMING AND
IN SOME INSTANCES NON EXISTENT, THE RECORDS OFFICE OF THE ROYAL AIR FORCE
AT RAF INNSWORTH WERE APOLOGETIC REGARDING THE LACK OF INFORMATION BUT DID
PROVIDE ME WITH MY SERVICE RECORD AND THIS INFORMATION WAS SCANT TO SAY THE
LEAST, I THEREFORE WENT BACK TO THE MoD IN WHITEHALL FOR FURTHER INFORMATION
AND ALSO FOR A COPY OF MY MEDICAL RECORDS. I AGAIN HAD A REPLY FROM THE PERSONNEL
MANAGEMENT AGENCY (ON BEHALF OF THE RAF) AT INNSWORTH AND THEIR CHIEF SECRETARY
INFORMS ME THAT ALL AIRMENS DETAILED RECORD OF SERVICE IS DESTROYED AFTER
6 YEARS OF END OF ENGAGEMENT (IN MY CASE 14/07/75) AND THAT BOARD OF INQUIRY
REPORTS ARE DESTROYED AFTER 20 YEARS AFTER THE INQUIRY WAS HELD (IN THIS CASE
SOMETIME IN 1980) . CERTAIN CONFIDENTIAL MILITARY DOCUMENTS ARE RELEASED TO
THE PUBLIC RECORDS OFFICE AT KEW AFTER 30 YEARS (THIS IS GENERALLY KNOWN AS
THE 30 YEAR RULE), HARRY HEYWOODS COUSIN DOREEN DID SOME RESEARCH HERE
AND AGAIN THE INFORMATION WAS VERY SCANT. SO TO SUMMARISE IF ANYONE TRIES
TO GET TO THE TRUTH ON ANY GOVERNMENT CONFIDENTIAL MATTER VIA OPEN GOVERNMENT
POLICY THERE ARE MANY OBSTACLES PUT IN YOUR WAY AND JUST WHEN YOU THINK YOU
ARE ABOUT TO CLEAR THE FINAL HURDLE, YOU FIND THAT MOST OF THAT INFORMATION
HAS GONE MISSING OR IS NONE EXISTENT . CURRENTLY THE DEPARTMENT OF THE SECRETARY
OF STATE FOR DEFENCE THE RIGHT HONOURABLE GEOFFREY HOON MP HAS HAD A LETTER
FROM ME ON THIS VERY SUBJECT AND I AM AWAITING HIS REPLY! I SUPPOSE THAT WAITING
30 YEARS, MEANS THAT EVERYONES MEMORY RECEDES WITH TIME , I CAN ASSURE
YOU IT DOESNT, IF YOU ARE DETERMINED THEN THE TRUTH IS OUT THERE
GO AND GET IT. I NOW HAVE OVER 200 DOCUMENTS RELATING TO THIS ACCIDENT AS
AT 30/06/2001 BEFORE 12/01/2001 I HAD NONE, I WAS MERELY A PASSENGER ON A
TRANSPORT AIRCRAFT OF THE ROYAL AIR FORCE THAT CRASHED INTO THE SEA FOR REASONS
NOT KNOWN.
I HAVE SINCE FOUND THREE OTHER PASSENGERS FROM THAT AIRCRAFT
ACCIDENT VIA A PLEA BY THE DAILY MAIL MISSING AND FOUND COLUMN
AND THEIR STORIES ARE ALSO VERY INTERESTING AND THAT THERE IS SOME BITTERNESS
RELATING TO THIS ACCIDENT FROM THESE GUYS. THE AUTHORITIES FOUND THAT THIS
COULD BE A RATHER EMBARRASSING INCIDENT TO THE SQUEAKY CLEAN IMAGE OF THE
ROYAL AIR FORCE, GET RID OF THESE GUYS, TELL THEM NOTHING AND THEY WILL FORGET
ALL ABOUT IT! THEY DIDNT BARGAIN FOR MYSELF DID THEY? TO NOT COMPENSATE
US THAT NIGHT FOR THE LOSS OF OUR PAY (AN ENTITLEMENT), TO ANY RECOMPENSE
FOR THE LOSS OF THEIR PERSONAL POSSESSIONS (NO ONE TOLD ME THAT I NEEDED TO
BE INSURED FOR SUCH AN ACCIDENT AND WAS WILLING TO CARRY MY PERSONAL POSSESSIONS
AT NO CHARGE). KD DRESS WAS WORN THAT NIGHT BY ALL ON BOARD AND WHITES
BY THE SAILORS NOW IF WE WERE GOING TO HAVE TOA SWIM THE LAST TWO MILES SHOULD
NOT SWIMMING TRUNKS BE THE DRESS OF THE DAY? WHY WERE ILL FITTING UNIFORMS
ISSUED AT NICOSIA, AND WHY WERE THE SURVIVORS PUT UP IN TENTS IN FREEZING
CONDITIONS, WHY WERE WE ALL WEARING TOWELS AROUND OUR NECKS (BECAUSE THE RAF
DID NOT SUPPLY FRONT AND BACK COLLAR STUDS) AND WHEN A SAILOR AS ONE OF THE
SURVIVORS SPORTING A BEARD IN RAF UNIFORM WITH NO HAT WAS ASKED BY A REDCAP
ARMY POLICEMAN AT SWINDON STATION AND WHOSE F*****G ARMY ARE YOU IN?
(AS RECALLED BY S.A.C. BRIAN WILMER A PASSENGER WITH US ON THE BRITANNIA),THE
WHOLE EPISODE BEGGARS BELIEF, OUR QUICK EXIT THROUGH CUSTOMS AND IN DAVID
BLOOMFIELDS CASE WHEN HE ARRIVED AT RAF WADDINGTON GUARDROOM TO REPORT
TO HIS NEW UNIT WAS CONFRONTED BY A SENIOR N.C.O. AS TO WHY HE WAS WEARING
CIVILIAN CLOTHING AND NOT UNIFORM, AND LATER HAD TO BUY HIS FULL UNIFORM FOR
£35 FOR SOMETHING THAT HAPPENED WHICH WAS NOT HIS FAULT! THIS IS THE
SQUEAKY CLEAN IMAGE OF THE ROYAL AIR FORCE.
THERE ARE MANY QUESTIONS STILL TO BE ANSWERED, THE NITTY
GRITTY QUESTION WHY DID IT HAPPEN HAS BEEN ANSWERED AND WE KNOW THAT
NEGLIGENCE BY PILOT ERROR WAS THE CAUSE AND AS YET STILL TO BE ADDRESSED.
MY INTENTIONS TO FLY AGAIN AFTER I LEFT THE SERVICE OF THE
R..A.F. HAS NEVER BEEN FULFILLED, I DO NOT HAVE THE CONFIDENCE TO TAKE TO
THE AIR AGAIN, TWICE BITTEN IS ENOUGH BECAUSE WITHIN 24 HOURS OF HASTINGS
TG579 CRASHING INTO THE SEA AT GAN WE TOOK THE WHITE KNUCKLE RIDE
ON THE 2ND MARCH 1960 AT KARACHI VIA A BRITANNIA XL638 SIRIUS,
WE LANDED AT KARACHI, REFUELLED, TOOK OFF WHEN WE HAD ANOTHER EMERGENCY IN
AS MUCH THAT A NOSE WHEEL ACTUATOR FAILED TO OPERATE RESULTING IN A
NOSE WHEEL RED, AT THE TIME OF THIS INCIDENT NO PASSENGERS WERE INFORMED
OF THE PROBLEM. I WAS SAT BY A WINDOW AND COULD SEE WHAT I THOUGHT WAS SMOKE
COMING FROM NUMBER THREE ENGINE, I STOOD UP IN PANIC AND CALLED THE CABIN
STAFF OVER (A SERGEANT) WHEN ALMOST IMMEDIATELY A MEMBER OF THE CREW (CAPTAIN?)
CAME OVER THE TANNOY SYSTEM TO SAY THAT WHAT WE WERE SEEING WAS FUEL BEING
JETTISONED AND WHAT LOOKED LIKE SMOKE WAS IN FACT ATOMISED FUEL. TERROR WENT
THROUGH MY BODY FOR ONE HOUR AND TEN MINUTES WHILST WE CIRCLED DUMPING FUEL
AND AIR TRAFFIC CHECKING THE UNDERCARRIAGE NOSE WHEEL WAS DOWN, I CANNOT BEGIN
TO EXPLAIN THE FEAR THAT I AND OTHER SURVIVORS ENCOUNTERED, THIS SPREAD TO
OTHER PASSENGERS NOT ASSOCIATED WITH THE HASTINGS INCIDENT. TWO OTHERS ON
THE BRITANNIA WERE JOHN BAWDEN AND BRIAN WILMER WHO HAVE MADE CONTACT AND
RECALL THE WHITE FACES AND KNUCKLES OF THOSE SURVIVORS AND HOW THE EMERGENCY
FIRE CREWS AND AMBULANCES LINED THE RUNWAY AND CHASED AFTER US WHEN WE TOUCHED
DOWN SAFELY! I SWEAR THAT IF I HAD BEEN GIVEN A PARACHUTE AT THAT TIME I WOULD
HAVE TAKEN THIS EASIER ROUTE OF ESCAPE.........................................
|